Keep Your Home Comfortable With Quality HVAC Services In Wallingford CT
X-Treme Temp Heating & Cooling is your go-to HVAC service provider in Wallingford, CT! We’re the experts in home comfort year-round, from AC and heating repair to ductwork and water heaters. We’ve got you covered from installation to maintenance so you can have peace of mind about your heating and air conditioning.
Read the reviews below from Wallingford, CT residents to see what your neighbors say about our expertise and customer service. We can’t wait to work with you!
Local Reviews
for Wallingford, CT
Customers say: The reviews reflect an overwhelmingly positive sentiment toward the HVAC service company. Customers consistently express high satisfaction with the technicians' professionalism, punctuality, and technical expertise. A recurring theme throughout the feedback is appreciation for clear communication, with many clients highlighting how thoroughly technicians explained problems, solutions, and repair processes in understandable terms. The service quality is repeatedly praised, with customers noting efficient troubleshooting, thorough maintenance work, and effective problem resolution. Many reviewers indicate strong loyalty to the company, mentioning they are repeat customers or plan to use the service again in the future. The overall tone is decidedly positive, with customers valuing the company's responsiveness, reasonable pricing, and the technicians' friendly demeanor. The reviews collectively portray a reliable HVAC service provider that delivers quality workmanship while maintaining excellent customer relations.
Our Reviews by City
Excellent work !!
Judy - Wallingford, CT 06492
Andrew is a fine representative of your company. He is thorough and efficient. I would recommend him and your company to anybody that asks. Thank you as always.
Always the best!
Joan - Wallingford, CT 06492
Such a great company! Dependable, knowledgeable and experienced, and at a fair price.
Excellent Service
Lagase - Wallingford, CT 06492
Technician is always awesome. Thorough and very polite.
Great service
Bob - Wallingford, CT 06492
Excellent experience. They are very good and very knowledgeable ,fixed the issue with my heater in a remarkably short time
Excellent service!
Doll - Wallingford, CT 06492
X-treme Heating and Cooling replaced our A/C and have been servicing our systems since we moved in six years ago. They are always professional, polite, responsive and reasonable. Highly recommend.
Excellent Service
Lia - Wallingford, CT 06492
Great service experience!
Pete - Wallingford, CT 06492
Thanks for the great service. Andrew was very professional and knowledgeable about our heating system. He provided great detail on how the system works and provided recommendations to improve it. Very much appreciated the timely service.
Service was excellent
MaryAnne - Wallingford, CT 06492
Excellent service
MaryAnne - Wallingford, CT 06492
Always a pleasure
Sam - Wallingford, CT 06492
Great service!
Eileen - Wallingford, CT 06492
As always Andrew and his apprentice were welcome professionals to our home. Communication, timeliness, expediency, neatness, and price all great.
Very satisfied
Piroska - Wallingford, CT 06492
Larry came on time, and fixed the problem quickly and professionally. I had excellent experience with him and I can’t thank enough to Lisa . Definitely recommend to anyone !!
Excellent service
Paul - Wallingford, CT 06492
Arrived on time. Appeared to know exactly what to do. Excellent and friendly service.
Great service!
Seamus - Wallingford, CT 06492
Larry was on time and very professional. They reached out ahead to confirm as well, which was nice. He provided the requested testing/tune up and was able to help with some minor issues that were discovered, right then and there. I would highly recommend.
Great service
Bill - Wallingford, CT 06492
Andrew got right to work. I observed that he was also sharing his knowledge with his helper.
Reliable, competent, and customer-oriented
Marisa - Wallingford, CT 06492
I’ve used Xtreme for all of my HVAC needs (new furnace, ductless and HW heater included. They are skilled, reliable, and straightforward. Their prices are transparent and reasonable
Larry provided excellent service
Lia - Wallingford, CT 06492
Always a true professional!
Eileen - Wallingford, CT 06492
It’s comforting to have a reliable, efficient, affordable and timely service provider who is additionally polite and friendly! Andrew and his apprentice were a pleasure to welcome into our home!
EXCELLANT service
Lori - Wallingford, CT 06492
These guys are great!
Suzanne - Wallingford, CT 06492
Not only are we customers, but I referred my son to them when he found himself without heat They responded quickly and were able to fix the problem right away for him
Terrific service
Jamie - Wallingford, CT 06492
Terrific service. He went above and beyond in servicing my furnace.
excellent service
rmiller7861 - Wallingford, CT 06492
Excellent Service
Brooke - Wallingford, CT 06492
Larry was very kind, knowledgeable, and friendly!
Excellent service
Otto - Wallingford, CT 06492
Thorough on time and explain the the results of the cleaning. Carried himself professionally, took the time to explained everything.👍
Excellent service
peter - Wallingford, CT 06492
Larry H.
I conducted a comprehensive preventive maintenance check on three air conditioning systems. This included blowing out the drain lines, inspecting and replacing air filters with the customer's assistance, and testing the condensate pumps. The condenser was rinsed, and I checked all electrical connections, pressures, and temperatures. All systems operated correctly. In the in-law unit, I identified low refrigerant levels, adding 10 oz of R410a to achieve optimal subcooling. The compressor side capacitor was below the manufacturer's rating, so I replaced it with a new one. After installation, I started and tested the system to ensure proper function.
Andrew H.
Heating Repair: Dispatched for loud vibration and weak airflow coming from the furnace during operation. Found the blower wheel out of balance and the motor mounting bracket worn loose. Re-secured the assembly, replaced the damaged bracket, and tested airflow and motor amperage. The furnace is now running quietly with proper air movement throughout the home.
Dyllan M.
Water Heater Repair: Customer reported popping noises from the water heater along with rusty-colored hot water at several fixtures. Inspection found heavy corrosion around the anode rod and significant sediment buildup inside the tank reducing heating efficiency. Replaced the worn anode rod, performed a full tank flush to remove sediment, and inspected the heating components for proper operation. Tested water temperature and pressure at multiple fixtures, and hot water is now running clean with improved recovery and quieter performance.
Jonathan L.
Heating System Repair: Customer reported the furnace was running in the evenings, but the house never seemed to reach the thermostat setting. Inspection found a weak inducer motor and a dirty flame sensor causing inconsistent burner operation. Cleaned the flame sensor, replaced the inducer motor, and tested several full heating cycles. The system now heats evenly and runs without interruption.
Larry H.
I conducted a comprehensive preventive maintenance service on the air conditioning system. I began by blowing out the drain line to ensure proper drainage. The air filter was checked and replaced by the customer. I then inspected and tested the condensate pump, confirming its functionality. The condenser was thoroughly rinsed to remove any debris. Electrical connections were examined, and system pressures and temperatures were checked for optimal performance. The EZ trap was found to be leaking at a fitting, so I replaced it and conducted a test to ensure it was functioning correctly. The system is now operating efficiently.
Larry H.
I conducted a comprehensive preventive maintenance service on the air conditioning system. This included blowing out the drain line to ensure proper drainage and replacing the air filters to enhance air quality. I also checked and tested the condensate pump, ensuring it was functioning correctly. The condenser was thoroughly rinsed to remove any debris. Additionally, I inspected all electrical connections, checked system pressures, and verified temperatures. The system is now operating efficiently.
Andrew H.
Upon arrival, I assessed the issue with the drain line, identifying a leaking union and a snapped PVC section at the air handler. The male adaptor had broken, and the gasket for the PVC union was pinched, preventing proper seating. Additionally, the union was slightly cross-threaded, complicating disassembly. I replaced the broken adaptor, installed a new PVC section and coupling, and replaced the damaged gasket. After testing the system with water, I confirmed the drain line was leak-free and functioning correctly.
Andrew H.
I conducted a thorough inspection of the indoor evaporator coil and blower compartment. All electrical connections and safety features were checked, along with voltage and amperage levels. The air filter was examined and found to be clogged, leading to coil icing. It was replaced with a new one. The condenser coil was rinsed, and the drain line was cleared to ensure proper drainage. The condensate pump, refrigerant levels, capacitor, and thermostat operation were also tested.
Andrew H.
I conducted a thorough inspection of the indoor evaporator coil and blower compartment, ensuring all electrical connections and safety mechanisms were functioning correctly. I measured voltage and amperage levels, visually inspected the air filter, and rinsed the condenser coil. The drain line was blown out, and water was poured to confirm proper drainage. The condensate pump was tested, and refrigerant levels were checked, revealing a slight deficiency. The capacitor was also inspected, and temperatures were taken. Thermostat operation was tested, and pictures and measurements were taken for a replacement quote. The customer is considering a 15 SEER option.
Andrew H.
I conducted a thorough inspection of the indoor evaporator coil and blower compartment, ensuring all components were functioning correctly. Electrical connections and safety features were meticulously checked, along with voltage and amperage levels. The air filter was examined for cleanliness, and the condenser coil was rinsed. The drain line was cleared, and a water test confirmed proper drainage. The condensate pump was tested for efficiency, and refrigerant levels were verified. The capacitor was inspected, and temperatures were measured. Finally, thermostat operation was tested to ensure accurate control.
Andrew H.
I conducted a thorough inspection of the indoor evaporator coil and blower compartment, ensuring all electrical connections and safeties were intact. I checked voltage and amperage, replaced the air filter with the customer-supplied one, and rinsed the condenser coil. I cleared the drain line and tested the condensate pump. After finding the condenser coil clogged with dirt, I performed a chemical clean with customer authorization, improving heat transfer efficiency. I also checked refrigerant levels, the capacitor, took temperatures, and tested thermostat operation.
Larry H.
Upon arrival, the customer reported that the condenser failed to start when the system was turned on, with the board displaying a 4-time flash indicating a hard lockout. I reset the unit, which successfully restarted the condenser. I then checked both cooling and heating pressures, confirming the system had the correct refrigerant charge with 12° of subcooling. When switching to heating, I jumped the terminals to initiate defrost, but the board did not respond. Given this issue, I recommend replacing the board before winter to prevent potential faults caused by the board's inability to switch into defrost during cold weather.
Andrew H.
I meticulously cleaned and inspected the burner tubes, ensuring they were free of debris. The burner, blower compartments, and surrounding area were thoroughly vacuumed. Electrical connections and safety features were checked for integrity. Gas pressures were verified, and the flame sensor was cleaned and inspected. Pressure switches were examined, and a combustion test was conducted, recording inlet pressure at 7.008 in.w.c., manifold pressure at 1.399 in.w.c., 11% oxygen, and 5ppm carbon monoxide.
Larry H.
I conducted a comprehensive preventive maintenance service on the air conditioning system. I began by blowing out the drain line to ensure proper drainage and prevent clogs. Next, I checked and replaced the air filter, which measured 14 inches by 24 inches by 1 inch. I then rinsed the condenser to remove any accumulated dirt and debris, enhancing its efficiency. Additionally, I meticulously checked all electrical connections for any signs of wear or damage. I also measured the system pressures and temperatures to ensure they were within the optimal range. Upon discovering that the system was low on refrigerant, I added 10 ounces of R41a to restore the correct levels. The system is now operating efficiently and effectively.
Andrew H.
I began by thoroughly inspecting the indoor evaporator coil and blower compartment, ensuring all components were clean and free from obstructions. I meticulously checked all electrical connections and safety mechanisms to confirm they were secure and functioning correctly. I measured the voltage and amperage to verify optimal performance. The air filter was visually inspected and replaced if necessary. I rinsed the condenser coil to remove any accumulated dirt and debris. The drain line was blown out and tested with water to ensure proper drainage. I checked the refrigerant levels to ensure they were within the manufacturer's specifications. The capacitor was tested for proper functionality. Temperature readings were taken at various points to assess system efficiency. Finally, I tested the thermostat operation to ensure it was responding accurately to temperature changes.
Larry H.
I conducted a comprehensive preventive maintenance check on the air conditioning system. This included blowing out the drain line to ensure proper drainage and replacing the air filters to enhance air quality. I also checked and tested the condensate pump to confirm it was functioning correctly. The condenser was rinsed to remove any accumulated debris. Electrical connections were inspected, and system pressures and temperatures were checked to ensure optimal performance. The system was found to be operating properly. Additionally, I identified that the capacitor was nearing its limit and replaced it, followed by starting and testing the system to confirm its proper operation.
Andrew H.
I began by carefully removing the sections of the supply and return pipes that had been incorrectly sized to 1 inch. I then installed 1 1/2 inch piping on both the supply and return lines to ensure proper flow and efficiency. Next, I removed the metal hole straps and replaced them with threaded rod to provide adequate support for the new pipes. I also replaced the autofeed and backflow combo to enhance system reliability. After filling the system with water, I conducted a thorough test to confirm that the unit was operating correctly. The job is now complete, and the system is functioning as intended.
Larry H.
I conducted a comprehensive preventive maintenance check on the air conditioning system. I blew out the drain line, checked the air filter, and assisted the customer in replacing it. The condenser was thoroughly rinsed. I inspected electrical connections, pressures, and temperatures, confirming the system's proper operation. Additionally, I replaced the condenser fan motor and dual capacitor, ensuring they started and functioned correctly. The customer requested a new thermostat for the upstairs area, to be relocated to the hallway, and an oil tank replacement with a Roth 275-gallon tank.
Andrew H.
We conducted a comprehensive maintenance check on the air conditioning systems. This included performing two preventive maintenance checks, inspecting the indoor evaporator coil and blower compartment, and ensuring all electrical connections and safety features were operational. We measured voltage and amperage, examined the air filter, and rinsed the condenser coil. The drain line was cleared, and the condensate pump was tested. Refrigerant levels were checked, and the capacitor was inspected. Temperatures were taken, and thermostat functionality was verified. We identified a slight refrigerant decrease in the main floor unit and added 8 oz of R22 after authorization. The second-floor air filter was found to be heavily clogged, potentially causing hair to reach the coil. We recommend monitoring the air filter and considering a unit replacement for the first floor due to rising compressor amp levels.
Larry H.
During the service, I thoroughly inspected the wiring and valve systems. Upon examination, the main house zone valve's stem was found to be partially depressed, preventing it from fully closing. Despite attempts to manually push it down, the valve remained unresponsive. With the valve in a partially open state, it was inadvertently closing the end switch, causing power to be sent back to the boiler and initiating its operation. Given the valve's condition, it is imperative to replace it before the onset of winter to ensure proper system functionality.
Larry H.
I conducted a comprehensive preventive maintenance check on the air conditioning system. This included blowing out the drain line, replacing the air filters with the customer-supplied ones, and rinsing the condenser. I also inspected electrical connections, checked system pressures and temperatures, and confirmed proper operation. Additionally, I adjusted the water heater temperature from 120° to 130°.
Larry H.
Upon activation, the air handler initiated but the lights dimmed, and the condenser remained off. Upon inspection, both capacitor sides were faulty, with zero readings on both the compressor and fan. Replacing the capacitor resolved the issue, and the system started correctly. The refrigerant charge was slightly low, so I added 5 oz of R22, achieving a 52°F discharge temperature. The condenser coil was cleaned, and the air filter, which was heavily clogged, was temporarily removed. A new filter will be installed by the customer.
Andrew H.
I thoroughly cleaned the condenser coil to ensure optimal heat transfer. All electrical connections and safety features were meticulously checked for integrity. Drain lines were cleared of debris, and water flow was tested to confirm proper drainage. Each cooling head was tested in high cool mode, producing air temperatures between 39-41 degrees. Voltage and amperage were verified to ensure electrical efficiency. The evaporator coils, blower compartments, and filters were inspected visually and cleaned. Filters were washed with water to remove any accumulated dirt. The unit is now operating efficiently.
Larry H.
Upon inspection, the zone valve for the main part of the house was found to be open, even with the thermostat removed. The power head was disconnected, but the valve remained open, indicating a faulty power head. After replacing the power head, the valve opened when the thermostat was turned on but failed to close when turned off, suggesting a short circuit. Despite the thermostat being disconnected, 24 volts were present at the valve terminals. Tracing the wires, a section was replaced, but the issue persisted. Further troubleshooting is required, and the power head will need to be replaced again.
Larry H.
I conducted a comprehensive preventive maintenance service on the air conditioning system. I began by blowing out the drain line to ensure proper drainage and replaced the air filters to enhance air quality. I then checked and tested the condensate pump, ensuring it was functioning correctly. The condenser was rinsed to remove any accumulated debris. I meticulously checked the electrical connections, pressures, and temperatures to confirm the system's integrity. Although the system was operating properly, I noticed the capacitor inside the condenser was below the manufacturer's specified limits. The capacitor, rated for 40/5 mfd +/-6%, was reading 32 on the compressor side. I recommended and subsequently replaced the capacitor, followed by starting and testing the system to ensure it was operating correctly.