Keep Your Home Comfortable With Quality HVAC Services In Wallingford CT
X-Treme Temp Heating & Cooling is your go-to HVAC service provider in Wallingford, CT! We’re the experts in home comfort year-round, from AC and heating repair to ductwork and water heaters. We’ve got you covered from installation to maintenance so you can have peace of mind about your heating and air conditioning.
Read the reviews below from Wallingford, CT residents to see what your neighbors say about our expertise and customer service. We can’t wait to work with you!
Local Reviews
for Wallingford, CT
Our Reviews by City
Excellent Service
Charles - Wallingford, CT 06492
Very professional, answered all questions asked.
Excellent Service
Cheryl - Wallingford, CT 06492
Would not use anyone else. Always receive superior service.
Excellent Service
Environmental - Wallingford, CT 06492
Thanks Larry for the quick response and service done on our water heater. Looks like we have a new company to service our heating and cooling systems!! Great job!!!
Highly recommend contacting X-treme for all your HVAC needs
Jeff - Wallingford, CT 06492
Furnace maintenance
Kimberly - Wallingford, CT 06492
Always professional and on time! Larry explains everything that is needed to be done and makes recommendations for the future of the furnace and water heater based on his observations
Excellent service
melanie - Wallingford, CT 06492
Excellent service very knowledgeable technician
Smart Thermostat Installation
Christopher - Wallingford, CT 06492
Needed a common wire installed to one thermostat and another installed and the both wired in correctly. He got the job done, was polite and professional. However, he told me it would be $307. for the work before starting. After it was finished he told me it took him longer so they charged me $360.86 Ok that’s fine, “nothing crazy”. I also explained I need the boiler serviced. Want to replace the beat up modern baseboard radiators upstairs, and want to replace three non working antique baseboards with “expensive” working ones. If your price changes on a small job why would I trust it on bigger projects? Simple fact is I wouldn’t, I’m going to call another company. Maybe I’m wrong on this but that’s my logic. Thanks for getting the Ecobees in for my anyway, cheers!
Great service
Dominic - Wallingford, CT 06492
Very professional
Great, thorough service
Sam - Wallingford, CT 06492
Professional service
Mark - Wallingford, CT 06492
Dylan was a pleasure to deal with. He was thorough and did everything he could to diagnose the issue.
Excellent service
Vendetto - Wallingford, CT 06492
Great service very professional
Oil pump
Roger - Wallingford, CT 06492
Thank you so much, Andrew was amazing, professional, and knowledgeable. I'm so happy that out of so many companies, we picked Extrem
Great service
Paul - Wallingford, CT 06492
Excellent Service
John Moher - Wallingford, CT 06492
Dyllan showed up on time exactly when he said he would. Dyllan explained what he was going to do to our furnace. The furnace was repaired in little over an hour and he and his partner cleaned up after the work as if they were never there. Dyllan, his helper, sorry I didn’t get his name, we’re great and did an Outstanding job. 5 Star Great Company
Outstanding overall outcome
Edward - Wallingford, CT 06492
Great customer service and professionalism when discussion how the technician was going to approach trouble shooting our HVAC concerns.
Good service
Jeffrey - Wallingford, CT 06492
Great Service
James.oneil@sbcglobal.net - Wallingford, CT 06492
Very attentive, quality work
Great service
Gina - Wallingford, CT 06492
Andrew did a great job, took his time and was very thorough!
Thorough
ashley - Wallingford, CT 06492
Awesome Service
Bob - Wallingford, CT 06492
Best company, they are reasonable, reliable & beyond courteous!
Amazing Service!!
Miriam - Wallingford, CT 06492
Dyllan was very professional and explained everything to me! My burner had been neglected and he got it cleaned out and running great!!! Highly recommend Extreme Heating and Cooling….and Dyllan!
Great service
patty - Wallingford, CT 06492
Very pleasant to work with will call back to get repairs
Great service
John - Wallingford, CT 06492
disappointed that the part replaced lasted just 3 months and we had to pay the labor cost a second time.
Andrew was very knowledgeable in his profession, did his job with great pride. Did an excellent job.
diana - Wallingford, CT 06492
New Filter and check heat balance in house
Karen - Wallingford, CT 06492
Andrew polite and efficient and professional. Good work!

Dyllan M.
Upon arrival I found there was no smell of oil in the house. Turned the unit on and found nothing wrong. The burner was reading 220 ohms which is very good. Combustion test was 0ppm. Walked through the house with my tester and found no traces of carbon monoxide with the unit running. I did find that there was a flex run that broke off of the ductwork. That flex line will need to be replaced because it’s too short now to reach the ductwork. I taped off the tap on the ductwork that was blowing hot air into the basement. the smell may have been coming fro there because it was blowing hot air right onto the insulation. The flue pipe is very thin and needs to be replaced. There were no holes in the flue pipe for my combustion analyzer which means the unit may not have been tested prior. I covered the new holes I made with silver tape which were giving off a smell because the tape was heating up. The smell will go away. Was not able to smell any concerning smells. The chimney has good draft

Dyllan M.
Found the zones labeled bed was very hot and the pump was not running. I loosened up the check valve and hit the side of it several times. Tightened the check valve back up and hit it a few more times. I also purged some water through that loop to get any loose debris out of the check valve. Turned on the boiler and watched it get up to temp. I now had 120*f before the check valve and 96*f directly after the check valve. A few feet down the line I had mid 60s. Before I did anything the whole zone was in the 120*f range. The check valve seems to be working and I was able to free it up. Recommend replacing the check valve. I included an estimate for the repair. 3/4” copper

Andrew H.
Visually inspected indoor evap coil and blower compartment Checked all electrical connections and safeties Checked volts and amps Visually inspected air filter Rinsed condenser coil Blew out drain line and poured water to ensure properly draining Tested condensate pump Checked refrigerant levels Checked capacitor Took temps Replaced 35/5 capacitor due to values being well under the factory specs.

Dyllan M.
Performed a mini split maintenance. Cleaned all the filters. Rinsed the condenser coil. Inspected and tested all drains. Tested each head. In max heat each head was putting out 115*f supply air. The rerun was 68-70*f. No issues found.

Dyllan M.
Performed a heating maintenance. Gas boiler. Cleaned the burner tubes. Removed flue pipe and cleaned off Debris. Cleaned the flame sensor. Inspected electrical. Found the boiler pressure was at 30psi. I put on my gauge and mine was reading 5psi. Started the boiler up and you can hear a lot of air in the pipes. Gas pressure was 3.36”wc. Combustion test was 1ppm at 9.5%o2. No other issues found. Included an estimate to replace the boiler gauge.

Larry H.
The pilot on the water heater was out, tried relating the gas for the pilot would not light. Blew out pilot tube, cleaned thermal pile , and adjusted spark igniter. Cleaned the main burner plate and vacuumed the bottom of the hot water heater where the air comes in for combustion. Started and checked operation. Cycled several times and the system is operating properly.

Larry H.
When arrived, the customer turned the system off due to the black smoke. System is plugged and needs to be cleaned. Replaced oil filter, nozzle, and strainer. Brushed out all the soot and removed the burner to clean the chamber. Started and performed combustion test. System is operating properly at this time.

Larry H.
Performed heating p.m. on gas boiler. Removed burners and cleaned and vacuumed. Cleaned flame sensor. Checked gas pressures, incoming 6.8”wc, manifold 3.4”wc. Performed combustion test. Performed an A/C PM on a Ductless system. Chemically rinsed condenser coil, checked and tightened electrical connections. Blew out drain lines on each unit. Checked System and heating, discharge temp was 120* f at each unit. While system was in AC temp was 50*f. System was drawing 5.7amps. System is operating properly. Chemically washed two indoor evaporator coils and blower wheels. Washed and 1Wiped down outer plastic housing.

Larry H.
Performed heating p.m. on oil furnace. Brushed and vacuumed. Replaced oil filter, nozzle, strainer and air filter. Replaced a small section of oil line that was showing signs of a leak and possibly causing the system to suck air in. The oil filter was very dirty. Checked safeties. Removed blower assembly and checked the blower wheel and motor for any play due to vibration which was noted on prior call. Found only one screw holding the blower tray in place, screwed the other side in and there is no more vibration when the blower turns on. System is operating properly. Performed a combustion test. The metal for the flue pipe is starting weaken , recommend replacing the flue pipe in the future.

Larry H.
Water was coming from the top of the extrol tank. Drain the pressure and replaced the extrol tank. Filled and purged the system. Turned the thermostats on and checked the operation. System is operating properly. The boiler is older, recommend replacing soon since it is a steel boiler and past its life span.

Larry H.
Perform PM on a gas boiler. Checked gas pressures, 6.87”wc coming in and 3.4”wc at the manifold. Performed a combustion test, 7.4 O2, 3 ppm CO. Checked the circulation of both zones. Resealed around the flue pipe going into the chimney. Checked the extrol tank and found that water is starting to migrate into the air side of the tank. Recommend replacing the tank and hi vent. There was also corrosion on the circulator gaskets for one zone, which should be replaced. Included a quote for making repairs. Also need to send a price over to the customer for replacing the cold water dip tube on the water heater.

Larry H.
Performed heating p.m. on oil furnace and oil hot water heater. Brushed and vacuumed. Replaced oil filter nozzles and strainers. Checked safeties, replaced air filter. Performed a combustion test.

Larry H.
Performed heating p.m. on an oil boiler brushed and vacuumed. Replaced oil filter nozzle and strainer. Started checked safeties and performed a combustion test. There are several areas that have calcium buildup from leaks, the domestic coil plate is deteriorating from a leak and unknown if the steel is pitted. Recommend replacing the boiler due to the age of the boiler and the cost of the repairs.

Larry H.
Burner was off on reset when arrived. Reset the control, the burner did not fire. Checked oil flow fuel line was full of air. Bled the line until clean oil came out of the pump. Burner started, cycled several times and let the boiler come up to temperature. There was a couple drips due to the boiler was cold, waited until the boiler warmed up and everything sealed properly no more leaks at this time system is operating properly.

Larry H.
When arrived the zone panel for the circulators were making a chattering noise, removed the relay for The indirect, the relay at the end direct was chattering. Removed 24 V to the relay on the indirect and noise stopped. Checked the zone panel to make sure there was proper operation with the priority setting and the other zones. Turned the water on to see if the aquastat for the indirect would turn on but it does not. The aquastat needs to be replaced. Picked up part and replaced the aquastat for the indirect hot water heater. Started and let the tank heat up with hot water until it satisfied the aquastat and turned on the other zones. System is operating properly.

Larry H.
Performed a heating p.m. on and oil boiler. Brushed and vacuumed the boiler, replaced the oil filter nozzle and strainer. Performed a combustion test. System is operating properly.

Dyllan M.
Upon arrival found the 0015 circulator pump inside the Weil McLain boiler had a loud noise to it when it turned on. Also found the circulator pump for zone 1 was making a winding noise as well. Customer wanted to replace both pumps. Drained down the system and replaced both circulator pumps. Filled and purged the system. Boiler got up to temp. Boiler is at 16psi. No water leaks. All zones came back hot.

Dyllan M.
Replaced the defrost board and the sensors it came with. Started and tested. After the delays the unit started up with no issues. I found the unit was low on refrigerant. Customer stated it hasn’t been serviced in roughly 10 years. May be a small leak starting to develop. Unsure at this time. Added 2lbs or r410a refrigerant. Unit required 11* up subcool. After I added the refrigerant I had 7-9* of subcool which is good. The inside temp was 59*f and after the unit ran for roughly 30min the temp was 66*f. I had 97*f supply temp air. Included the cost for the previous visit in today bills.

Larry H.
Upon arrival, the burner was off on reset. Reset the control and the burner started then went off on reset. Checked oil flow and transformer which were correct, checked the cad cell eye which had no reading causing the control to go off on reset. Replaced the guy and checked the readings. The cad cell eye was reading 1000 ohms. Replaced the nozzle which was dirty started and tested. The cad cell is now reading 513 ohms and operating properly.

Andrew H.
Upon arrival unit was running and had a large amount of air in the lines. Pressure was displaying at 40psi on the pressure gauge which is too high. Drained pressure and saw the pressure gauge was reading 15psi higher than the real pressure. Replaced the pressure gauge with a new one. Also added ball valves and new boiler drains on the return so the zones could be bled of air properly. Filled the boiler back up and bled all zones of air. Started and tested unit. Had hot water coming back from both returns and had no air in the lines. Unit is working properly.

Dyllan M.
Upon arrival I found the unit was off on reset. Found the nozzle assembly was covered on carbon build up. Replace the oil nozzle and cleaned the assembly. Attempted to clean access oil out of the fire chamber. Noticed there was no liner in the chamber and oil had seeped through the gaskets of the boiler. Purged the oil line and started and tested. The unit fired up with no issues. Combustion test was 4.4%o2 at 17ppm. Also found the boiler was at 29psi. I found the expansion tank is bad and the internal bladder has water seeping through it. Customer denied replacement of the expansion tank. System is up and running. All returns came back hot.

Dyllan M.
Upon arrival I found water on the floor around the front right corner of the boiler. When the boiler turns on and heats up I found water coming out of a hairline crack in the front section of the boiler. Customer would like a quote for a new section.

Dyllan M.
Replaced two customer supplied tstat. Eco bee thermostats. Had to run a new section of wire for the first floor. Had to wire up commons for the thermostats. Started and tested. Both zones work properly. They turn the system on and off as needed. Customer will be calling to set up a a quote for new baseboard.

Dyllan M.
Upon arrival I found the customer had put a container under the burner. It had some oil in the pan. There was a coupling in the oil line that was saturated with oil. I tightened the coupling. Also found oil o the bottom of the burner. The nozzle assembly was saturated in oil. Replaced the oil nozzle. No active leaks found. Started the system. Recommend a cleaning.

Dyllan M.
Performed a heating maintenance. Oil boiler. The boiler is old. Changed the nozzle filters and strainers for the water heater and boiler. Cleaned the flue pipes and heat exchangers. The top Clean out plate for the boiler is cracked. I applied furnace cement to the crack. Recommend replacing the system in the future. Purged the oil line. Started and tested. Combustion test. Both units were under 10ppm. The boiler was 8.2%o2 and the water heater was 5.3%. No smoke on the smoke tests.